TEAM COTTON'S PERFORMANCE TURBO BUICK ONLINE FORUMS  

Go Back   TEAM COTTON'S PERFORMANCE TURBO BUICK ONLINE FORUMS > Technical Forums > Buick Turbo Tech
Register FAQ Community Calendar Today's Posts Search

Buick Turbo Tech General technical support for the 86-87 Buick turbo cars

Reply
 
Thread Tools Display Modes
  #11  
Old 11-17-2010, 05:53 PM
JCotton1's Avatar
JCotton1 JCotton1 is offline
Married Man
 
Join Date: Nov 2007
Location: Paradise
Posts: 1,434
Default

Quote:
Originally Posted by phagen28 View Post
Ok finally got back out in the car. With the regapped plugs the skip before the 1-2 shift is fixed,(more power now than anytime since I've had the car) thanks.I had already ordered a new wastegate solenoid from GM, locally. I ordered and put in GM p/n 1997227. which is listed for a deisel truck. made a plug adapter for it that would fit the male pins on the factory plug and then go on to the new sol. which also has 2 pins. I have also ordered an already made up adapter harness.this now gives me 14-15 lbs of boost now getting no K/R most times and maybe 1.2 deg some other times.as well as my question about the TPS on my prev post, I also wonder why I would get a different reading from the IAC sometimes.(always warmed up to 160 deg at idle). had it set to 20 with the TPS set to .44 with key on engine off, ran the car to work and came home, checked the numbers again when I got home and had IAC reading of 46. does this indicate that it needs cleaning and/or maybe a new one.
thanks for any advice
Paul
Sounds good, making progress... the IAC sounds like it is in the ballpark. In gear it tends to rise a little in park it is lower.. cleaning is a good idea if you haven't done it..
__________________
Jack Cotton
Cottons Performance
413-789-0531
Reply With Quote
  #12  
Old 07-18-2011, 04:02 AM
phagen28 phagen28 is offline
Junior Member
 
Join Date: Oct 2010
Posts: 8
Default knocking again

Back to the forum with another knock situation. My car has been running great. Plenty of power with little or no knock retard on the Scanmaster. I still have not been able to get much boost over 12lbs.
Now I had a problem with the battery and had to replace it. Since the battery replacement, I seem to have alot of K/R at almost anything over 1/2 throttle.
I am wondering if The computer will have to be readjusted with regard to the chip. My chip has been identified on an earlier post in this thread.could this be a possibility? maybe it's lean now or something like that. I will post a new set of numbers but am just trying to see if I'm thinking of something that is a possibility.
thanks
Reply With Quote
Reply

Bookmarks


Posting Rules
You may not post new threads
You may not post replies
You may not post attachments
You may not edit your posts

BB code is On
Smilies are On
[IMG] code is On
HTML code is Off

Forum Jump


All times are GMT. The time now is 06:05 AM.


Powered by vBulletin® Version 3.8.4
Copyright ©2000 - 2024, Jelsoft Enterprises Ltd.