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ET's and MPH Post up your track experiences. ET and MPH, what's your combo...

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  #11  
Old 07-09-2009, 04:33 AM
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PaceCarTA PaceCarTA is offline
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yeah i know i guess seeing as how its done it for the past 5 years and close to 600 passes i should be concerned
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Paul... NJ rep MAGNABUICK.com
the 86 3450lbs ...1.44 6.19@112 9.72@138 ,
109 234cu stock mains and bolts , irons,
the 87 ttop ,1.37 6.0@ 114 9.45 @ 141.9 25 psi !!
109 235cu .gn1 alum, certified roll cage .
the 87gnx'd FAST B2B TA49 ..back to all stock original #s 109 and trans hipro w stagerite
the 87 GN ttop ..all stock with vac brakes
86 WH1 mini tubbed roll caged 109, extreme 2004r
all on pump 93 and alkycontrol
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  #12  
Old 07-25-2009, 11:36 PM
86granny 86granny is offline
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Quote:
Originally Posted by twinrats View Post
WOW! 10's on a stock bottom end! Good Luck...you're going to need it. I hope it stays together for you.
The good Doc will keep that monster together he has forgot more than i will ever know about an LC2. You have that thing flyin Paulie good job
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  #13  
Old 07-22-2011, 08:34 PM
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happened upon this this old thread on a google search , didnt find what i was looking for

but figured i might as well update

about 4months after the last post the stock piston (#3) decided to split across the top , might have been that way for a while but waited till i had the tune rocking to become a hole
the run that it showed up on was at 24psi and was running 6.67 102.4 1/8 when it let go (started pushing oil out the breathers) and finished at 10.52 124.6 with a 1.48 60'

pulled the motor and I pressed off the cracked piston and pressed on a used stock piston using the old rod and rings , and then dropped in a fully assembled stock 109 motor i had on the stand (all stock turbo parts but with a NA crank)
that thing went 12.5 on stock turbo at 19psi
took a while to get the motor back together because ive been busy but i must have had a break as at some time I replaced the rod and main bearings and also replaced the #3 main cap that somehow got cracked ,

fast forward to march 2011. i decided to put the motor back together with really nothing changed about the motor..
same hyd flat cam/lifters (little 206) , same iron heads , same intake setup reused the cometics again (they were used ones from Jacks pile) I did upgrade the pushrods from stock to comp magnums and went with a stock balancer and flywheel and added a set of TA mild steel race headers

took it right to atco and ran 128
took it to etown 4-29 and turned out a 10.58 at 128.5 at 23psi



that should have been good enough but i really didnt want to spin this motor over 6K even though it pulled easily over 6350rpm on the shifts but trapped at 6000+ rpm so i wasnt about to push harder though im sure there was much more left

i had a forged roller motor in the works but couldnt get it ready for march
109 block bored to .020
JE .020 forged pistons
K1 rods
cat 4340 forged crank (std mains/ had to cut rods to .010 )
rotating assembly balanced for external
BHJ balancer ext
cat sfi flywheel ext
8445 irons with only cleanup behind valves ,no runner porting
comp 918 behives- locks- retainers
cut the exhaust guide down and teflon seals
cut the pedestal sides down for rolller rocker clearance
215/220 comp roller/comp lifters/comp magnum 8.150 prods /comp timing set
arp 12pt head studs
cometic 050 gaskets
T+D 155 roller rockers (.519intake- .529 exh) preload at .030
champion (buick-6) valve covers
stock intake but has the egr tower milled and filled
stock fuel rail and fuel lines accufab regulator
83# low Z inj
rtx injector hotwire
mease sheetmetal plenum (65 mm opened up to 70 barely)
accufab 70m TB
finished it off with TA perf stainless race headers


I pulled stock bottom end motor out and dropped that into my 87 and then dropped this one in ,
first night after a few test runs it ran 103.5 1/8 128.8 at under 22psi but couldnt hook on drag radials so best et was only a 10.81
went back the next week and even though it was hot it still put down 129.90 at 10.7 , still no traction
so i went back again last week with some slicks
still couldnt hold traction on a friday night prep but managed 104.25 1/8 and 130.0 through traps
and then upped the bost a wee bit and slipped the tires even worse 60' was 1.689 ran 103.8 and 130.75 @ 10.6 ,
boost was 22.6 through to the 1/8 then 23.6 to the top

keep in mind this is just a std 109 with no steel caps , no studs , no girdle , no hard blok just stock main caps and bolts , didnt even do a line bore
__________________
Paul... NJ rep MAGNABUICK.com
the 86 3450lbs ...1.44 6.19@112 9.72@138 ,
109 234cu stock mains and bolts , irons,
the 87 ttop ,1.37 6.0@ 114 9.45 @ 141.9 25 psi !!
109 235cu .gn1 alum, certified roll cage .
the 87gnx'd FAST B2B TA49 ..back to all stock original #s 109 and trans hipro w stagerite
the 87 GN ttop ..all stock with vac brakes
86 WH1 mini tubbed roll caged 109, extreme 2004r
all on pump 93 and alkycontrol

Last edited by PaceCarTA; 07-22-2011 at 10:03 PM.
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  #14  
Old 07-22-2011, 09:04 PM
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JCotton1 JCotton1 is offline
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Nice stuff Paulie, yyou guys bringing that stuff up to LVD tomorrow for the Buick race...
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  #15  
Old 07-22-2011, 10:33 PM
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im not looking forward to the bake in a black car in a staging lane , if i do go out it will be to run the efi points at etown
hopefully Griz can carry the buick flag high for us
and good luck with the pumpkin ,

ps, just remembered i have some fixing to do
came home to find on my atr ext pipe that the pipe going to the HKS wastegate was cracked at the inlet flange , i can weld it back but would rather move up to one of those pw46 gates , did the pw46 for a buddy on the same ATR DP last week and i beleive that was the last one you had in stock,
__________________
Paul... NJ rep MAGNABUICK.com
the 86 3450lbs ...1.44 6.19@112 9.72@138 ,
109 234cu stock mains and bolts , irons,
the 87 ttop ,1.37 6.0@ 114 9.45 @ 141.9 25 psi !!
109 235cu .gn1 alum, certified roll cage .
the 87gnx'd FAST B2B TA49 ..back to all stock original #s 109 and trans hipro w stagerite
the 87 GN ttop ..all stock with vac brakes
86 WH1 mini tubbed roll caged 109, extreme 2004r
all on pump 93 and alkycontrol

Last edited by PaceCarTA; 07-22-2011 at 10:40 PM.
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  #16  
Old 10-27-2011, 01:56 AM
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PaceCarTA PaceCarTA is offline
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Join Date: Dec 2007
Location: central NJ
Posts: 50
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thought id update this ..
ive been making changes but havent had the opportunity to get out and try them with the weather being so uncooperative

changes were because the power was coming in way to quick and couldnt get the car to hook , i had added co2 assist to the wastegate and that seemed to make it worse , even the ramps werent helping much

suspension was just stock upper arms , welded stock lowers and old 3way AVO shocks ....swapped them out for umi dbl adj poly uppers and umi box poly lowers , comp eng 3way adjustable shocks set 90/10 front and 50/50 rear .
installed a TA girdle rear cover with cap studs knowing once it hooks its going to be brutal
relocated the battery to the trunk with flaming river remote shutoff (nhra legal) which allowed me to put the alky bucket where the battery was and rear face the outlet because logs were showing that it was cavitating top of 1st gear , also replaced my 8yr old alky controller because it was no longer working progressively

fixed my PI gnx cluster vdo fuel level gauge and once again could see the actual level so i topped the tank off with 93 at quik chek

and also added a bailey two step to get a better handle on the launch to allow me to launch below my gate spring (8psi) if the track wasnt hooking

finally
efi event sat 10-22-11
nice weather for a change , no rain , mid 60s da 500-600ft 12mph wind (4 headwind) but what can ya do
sun was out and friday night was hooking great
old worn mickey 275/60-15 drs at 18psi , weight now with the battery kit and the full tank put the car at 3590 according to etowns new scale

1st pass set controller at 23psi and (ran 22 most of run)
forgot i had set a ramp to stage 1 on the msbc-1 (had ramp 10 )
had the baily two step set at 3200 launched at 6 even though it could go to 8 with the spring , and i remembered to turn the co2 on

time trial #1
1.649
4.403
6.737
104.73
8.871
10.501
130.12


it hooked so that was cool and the best et on this motor thus far , now to put a little more down

time trial #2
removed the ramp and set two step to 3600, launch control to 9psi
was a little rich up top at 10.5 a/f (target 10.8) so i tweaked the ve
and upped the boost stages to 24 (never went over 24 )

1.442
4.155
6.453
106.37
8.457
10.162
131.92



on to eliminations
dial a 10.22 figuring id use the brakes
.031 RT
1.469
4.160
6.453
106.61
8.455
10.163
131.33

i lifted 9 seconds in and still broke out

keep in mind this is on 93 and alky (methanol) injection at 20 degrees timing
stock fuel lines and rail ... thats going to change soon on the next upgrade
__________________
Paul... NJ rep MAGNABUICK.com
the 86 3450lbs ...1.44 6.19@112 9.72@138 ,
109 234cu stock mains and bolts , irons,
the 87 ttop ,1.37 6.0@ 114 9.45 @ 141.9 25 psi !!
109 235cu .gn1 alum, certified roll cage .
the 87gnx'd FAST B2B TA49 ..back to all stock original #s 109 and trans hipro w stagerite
the 87 GN ttop ..all stock with vac brakes
86 WH1 mini tubbed roll caged 109, extreme 2004r
all on pump 93 and alkycontrol

Last edited by PaceCarTA; 10-27-2011 at 02:36 AM.
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  #17  
Old 10-29-2011, 11:27 PM
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PaceCarTA PaceCarTA is offline
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Join Date: Dec 2007
Location: central NJ
Posts: 50
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minor update
fri night drove into track , teched and got in line with them telling me they werent going to run gamblers or realstreet 1/4 mile but rather only 1/8th mi , and the track was going to allow the street cars to run 1/4 but might change their mind as the night cooled so test and tune it was going to be
same tune as last week no changes

broke the tires loose through 1st
60' 1.694
330' 4.555
1/8 6.882
MPH 105.630
11000' 8.893
1/4 10.599
MPH 131.82

not happy but the trap mph was good
with tires still warm got right back in lanes and right back up to the tree only change i made was to drop the two step limit to 3100 figuring even a 1.5 would be ok as long as it didnt break loose

R/T .047
60' 1.488
330' 4.189
1/8 6.475
MPH 107.100
1000' 8.464
1/4 10.156
MPH 133.04

that was fun and a new personal best 1/8th and 1/4 on 93 and alchy


went back to make another pass before it got too cold , added 1 psi to the the stages for the middle of the track and sure as SHi# someone blew up in right lane at the top and stayed in the groove , 1 1/2 hrs of cleanup and the track made the decision to hold all cars to 1/8th mile passes so i called it quits , good thing because three cars later they oiled down the 1st half of the left lane and switched to right lane only 1/8mile passes
Oh well have to hope for nicer weather than this snow crap for a chance at a nine slip
__________________
Paul... NJ rep MAGNABUICK.com
the 86 3450lbs ...1.44 6.19@112 9.72@138 ,
109 234cu stock mains and bolts , irons,
the 87 ttop ,1.37 6.0@ 114 9.45 @ 141.9 25 psi !!
109 235cu .gn1 alum, certified roll cage .
the 87gnx'd FAST B2B TA49 ..back to all stock original #s 109 and trans hipro w stagerite
the 87 GN ttop ..all stock with vac brakes
86 WH1 mini tubbed roll caged 109, extreme 2004r
all on pump 93 and alkycontrol

Last edited by PaceCarTA; 10-30-2011 at 12:18 AM.
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  #18  
Old 11-26-2012, 03:43 AM
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PaceCarTA PaceCarTA is offline
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Join Date: Dec 2007
Location: central NJ
Posts: 50
Default In da nines

made some changes since last post
ptc 9.5 converter
ran some 10.11-10.12 runs at 108 .134.6 but 60 wasnt there and at top of track it was wandering
this required hitting it harder off the line and
found the umi lower control arm bushing had split from hard launching
so time for some rear suspension upgrades

wolfe racecraft upper and lower dbl adjust control arms
HR lower arm frame pocket braces (weld in)
QA1 single adjust rear shocks
12-150 2.5"coil springs on wolfe adjustable spring perches

notched the frame rails for some big meats (just outer rail)
15x10 weld alumastars and 325/50 MT radials
15x4 weld alumastar and 165 fronts

at 134 mph the stock lines were about due for an upgrade so
steel braided teflon lines , -8 feed and -6 return (stock rail with 8an bung)

also had overshoot running the msbc-1 in manifold mode even with the co2 assist
so i replumbed in wastegate mode and added a 2psi hobbs to activate controller
installed the PW46 gate (from Jack) on my atr 3" external pipe and .installed a 4.5 psi spring
also running baileys 2 step which also works good for the rev limiter as it cuts ignition not fuel

went to atco buick vs ford today and right off the trailer ran 1.529 110 9.96 136
made 4 more passes getting faster in the nines with a 1.52 9.974, 1.45 9.877 , 1.46 9.876 , and 1.448 9.827 at 136.79

stayed after for some time shots and upped the launch boost and spun 1.8 60' and 10.3 but at 137.23 !
mph showed id have a nice pass if it had stuck so i backed launch settings down where it was in time shots and the last pass was...

1.46 6.25 @ 110.97 9.815 @ 137.68

still pump gas 93 and methanol injection ,
18.5 deg timing
launched at 9.5psi (and 4100 on two step) and ran at 26.5 psi boost
__________________
Paul... NJ rep MAGNABUICK.com
the 86 3450lbs ...1.44 6.19@112 9.72@138 ,
109 234cu stock mains and bolts , irons,
the 87 ttop ,1.37 6.0@ 114 9.45 @ 141.9 25 psi !!
109 235cu .gn1 alum, certified roll cage .
the 87gnx'd FAST B2B TA49 ..back to all stock original #s 109 and trans hipro w stagerite
the 87 GN ttop ..all stock with vac brakes
86 WH1 mini tubbed roll caged 109, extreme 2004r
all on pump 93 and alkycontrol

Last edited by PaceCarTA; 12-15-2012 at 02:59 AM.
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  #19  
Old 11-27-2012, 11:37 AM
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JCotton1 JCotton1 is offline
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Great job Paulie!! That's haulin the mail. Inch by inch is a cinch.
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Cottons Performance
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  #20  
Old 11-12-2013, 07:18 PM
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PaceCarTA PaceCarTA is offline
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Location: central NJ
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little update
11-20-13 buick vs ford at atco
couple changes
bailey tr6 ignition
71hpqhp .85 (3 bolt)
ATR 3" dual pitbull exhaust
tubular uppers,
alum drums,
28x10 slicks on 10" alumastars
and removed about another 70 lbs from the car

should be around 3430 3/4 full tank with driver

1st pass , lost the line to the boost controller map sensor so no co2 assist
ran 13.0 105 at 4-8psi at top

fixed line

2nd time shot now warmed up to 50s but had a steady 20-30 mph head cross wind
1.440
4.027
6.212 @ 112 16
8.112
9.732 @ 139.16 best mph to date

the wind at top end ripped off my window mldgs on passsenger side and top
heres the vid
http://www.youtube.com/watch?v=vSKzv7ej7Cc

3rd time shot
1.447
4.017
6.194 @ 112.22
8.099
9.729 @ 138.13 best et to date


dialed 10.0 on elims ,lifted and broke out
1.42 9.882@ 137.79
__________________
Paul... NJ rep MAGNABUICK.com
the 86 3450lbs ...1.44 6.19@112 9.72@138 ,
109 234cu stock mains and bolts , irons,
the 87 ttop ,1.37 6.0@ 114 9.45 @ 141.9 25 psi !!
109 235cu .gn1 alum, certified roll cage .
the 87gnx'd FAST B2B TA49 ..back to all stock original #s 109 and trans hipro w stagerite
the 87 GN ttop ..all stock with vac brakes
86 WH1 mini tubbed roll caged 109, extreme 2004r
all on pump 93 and alkycontrol

Last edited by PaceCarTA; 02-27-2014 at 01:28 AM.
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