Thread: As always.....
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Old 10-18-2009, 03:48 PM
trbochrgd1's Avatar
trbochrgd1 trbochrgd1 is offline
I can't drive 55!
 
Join Date: Nov 2007
Location: North Jersey
Posts: 518
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Yes, it was the turboflange gasket. I ran a Wednesday a couple of weeks ago and it ran pretty good the first pass, 9.62 @140.11 60' 1.37,22 psi . I was in such a rush that morning that I unfortunelty forgot the laptop... So I only had one shot at recording a run. I got back to the pits checked everything over, called Jack, and then checked the plugs. Everything looked pretty good. I went up for another pass and It left very soft, with no boost, the top of first gear it was like a rocket booster kicked in and it took off! I don't have the timeslips in front of me but it was a low 10 second run at 137 mph. So I got back to the pits, it was pitch black out at this point and I was by myself. I check everything over the best I could and I found the vacuum port on the fuel pressure regulator that was loose. I tightened that and thought that was it. Went up again and it was just as bad as the second pass. So I put it back in the trailer and didn't touch it till Sunday. I started it up Sunday in the trailer and noticed a loud noise from the turbo area. As you can see the gasket was blown out! Thank goodness, because I thought my converter was fried... I'm just waiting for the gasket right now and a new thermostat (it was running a little hot).

Hopefully we get a chance to go out one more time this year.
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87 GN, RPE built 109 stroked, RJC girdle, billet main caps, custom comp roller cam, Champion ported aluminum heads, Champion aluminum intake, T&D 1.65 rockers, 96 lb injectors, Accufab 70mm throttle body RJC pullies, RJC A/C bracket,GTK-850, ATR headers,Deeds electronic boost controller, Cotton’s 4 inch down pipe w/ Turbonetics RG 45 gate, XFI, Cotton’s front mount, Level 10 built 400 trans w/brake, Converter? ,33 spline Moser axles, Spool, HR bar.

New best 9.44 @ 143!
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